Emissions were too high - Omex sent a new calibration map / Lamda probe, also replaced plugs, leads and coil pack to cure misfire, checked at local MOT garage.
Exhaust noise was above the 99db threshold - hopefully connected to above emissions and misfire
Parking brake needs adjusting as there's too much travel on the handbrake and the braking power wasn't strong enough - adjusted (this involved removing tunnel carpet)
Speedo was over reading - adjusted pulse setting to -15% of 'correct' setting
Full beam headlight on one side wasn't changing over properly (sticky solenoid) - cleaned solenoid and adjusted lights at local MOT garage
Gear box earth cable not connected
Rear view mirror vibrates - replaced mirror with dash mounted one
Starter motor electrical connections require rubber terminal boots - covered
Hopefully this is enough to satisfy the tested - re-test booked for Monday 11th July
I had to be at the Southampton test centre at 8.00 so I set of at 7.00, it was raining so I had a damp, chilly drive in. Unfortunately the car failed on number of counts including:
Emissions were too high
Exhaust noise was above the 99db threshold
Parking brake needs adjusting as there's too much travel on the handbrake and the braking power wasn't strong enough
Speedo was over reading
Full beam headlight on one side wasn't changing over properly (sticky solenoid)
Gear box earth cable not connected
Rear view mirror vibrates
Starter motor electrical connections require rubber terminal boots
You're not allowed to take photos in the centre so please don't tell anyone.