- Emissions were too high - Omex sent a new calibration map / Lamda probe, also replaced plugs, leads and coil pack to cure misfire, checked at local MOT garage.
- Exhaust noise was above the 99db threshold - hopefully connected to above emissions and misfire
- Parking brake needs adjusting as there's too much travel on the handbrake and the braking power wasn't strong enough - adjusted (this involved removing tunnel carpet)
- Speedo was over reading - adjusted pulse setting to -15% of 'correct' setting
- Full beam headlight on one side wasn't changing over properly (sticky solenoid) - cleaned solenoid and adjusted lights at local MOT garage
- Gear box earth cable not connected
- Rear view mirror vibrates - replaced mirror with dash mounted one
- Starter motor electrical connections require rubber terminal boots - covered
Hopefully this is enough to satisfy the tested - re-test booked for Monday 11th July
No comments:
Post a Comment